Girish Mahajan (Editor)

CSX 8888 incident

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Time
  
12:35 p.m.

Type of incident
  
Unmanned train

Trains
  
CSX freight train

Total number of deaths
  
0

Injuries
  
1

Country
  
United States

Cause
  
Operator error

Date
  
15 May 2001

Operator
  
Crew count
  
0

A yellow and blue CSX 8888 railway engine passing the road

Location
  
Walbridge – Kenton, Ohio66 mi (106 km)

Similar
  
San Bernardino train disa, Gare de Lyon rail accident, Great Train Wreck of 1918, 2008 Chatsworth train colli, Ryongchon disaster

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The CSX 8888 incident, also known as the Crazy Eights incident, was a CSX Transportation freight train in the U.S. state of Ohio in 2001. Locomotive #8888, an EMD SD40-2, was pulling a train of 47 cars including some loaded with hazardous chemicals, and ran uncontrolled for two hours at up to 51 miles per hour (82 km/h). It was finally halted by a railroad crew in a second locomotive, which caught the runaway and coupled to the rear car.

Contents

A yellow and blue CSX 8888 railway engine passing the road

The incident inspired the 2010 motion picture Unstoppable.

As of 2017 #8888 is still in service, having been rebuilt and upgraded into a SD40-3 as part of a refurbishment program carried out by CSX.

CSX 8888 incident CSX 8888quotCrazy Eightsquot WVNC Rails

Timeline

A yellow and blue CSX 8888 railway engine on the railroad

On May 15, 2001, a CSX engineer was using Locomotive #8888 to move a string of freight cars from one track to another within Stanley Yard in Walbridge, Ohio, CSX's primary classification yard for Toledo. The string consisted of 47 freight cars, 22 of which were loaded. Two tank cars contained thousands of gallons of molten phenol, a toxic ingredient of paints, glues, and dyes that is harmful when it is inhaled, ingested, or comes into contact with the skin.

A yellow and blue CSX 8888 railway engine passing the road

A 35-year veteran with a clean disciplinary record, the engineer noticed a misaligned switch and concluded that his train, although moving slowly, would not be able to stop short of it. He decided to climb down from the train, correctly align the switch, and reboard the locomotive.

Railway engine CSXT 8029 is waiting for another train at the siding at Tunnel Hill, Georgia, on the Western and Atlantic Sub

Before leaving the cab, the engineer applied the locomotive's independent air brake. During mainline operation, he would also have applied the automatic air brake, setting the brakes in each of the train's cars. But, as is normal for intra-yard movements, the air brakes of the train were not connected to the locomotive, and thus were not functional. Furthermore, applying the locomotive's brakes disabled the train's dead man's switch, which would otherwise have applied the train brakes and cut the engine power. The engineer also tried to apply the locomotive's dynamic brake, but failed to do so. He then set the throttle for the traction motors at 100%. If the dynamic brakes had been selected as intended, this throttle setting would have caused the train to slow down. However, since dynamic braking was not engaged, the setting caused the train to accelerate. Therefore, the only functioning brake was the air brake on the locomotive, and this was not enough to counteract its engine power.

Map of the railway engine CSX 8888 incident. The train's path highlighted in blue

The engineer climbed down from the cab, then attempted to reboard the accelerating locomotive. He was unable to do so and was dragged about 80 feet (24 m), receiving minor cuts and abrasions. There were no other injuries or deaths resulting from the incident.

The train rolled out of the yard and began a 66-mile (106 km) journey south through northwest Ohio with no one at the controls.

Attempts to derail the train using a portable derailer failed and police shot at an emergency fuel cutoff switch, which had no effect because the button must be pressed for several seconds before the engine is starved of fuel and shuts down. A northbound freight train, Q63615, was directed onto a siding where the crew uncoupled its locomotive, #8392 (another EMD SD40-2), and waited for the runaway to pass. #8392 had a crew of two: Jess Knowlton, an engineer with 31 years of service; and Terry L. Forson, conductor with one year's experience. Together, they chased the runaway train. An EMD GP38 locomotive was prepared further down the line to couple to the front of the runaway to slow it further, if necessary.

Knowlton and Forson achieved a connection to the last car of the train and managed to decelerate it by activating the dynamic brakes on their pursuing locomotive. When the speed of the runaway train decreased to 11 miles per hour, CSX trainmaster Jon Hosfeld matched its pace on foot, boarded the train, and deactivated the engine. This intervention brought the train to a halt just southeast of Kenton, Ohio, preventing it from reaching the GP38 locomotive. Due to the continuous application during the incident, all the brake blocks on locomotive #8888 were rendered useless by the excessive heat generated.

The name of the engineer who let the train slip was never made public.

Preservation attempts

Several railway museums have tried to buy No. 8888, but CSX officials replied that they did not feel the locomotive worthy of preservation, and that it would be rebuilt as part of the SD40-3 rebuild program in late 2014 and early 2015.

References

CSX 8888 incident Wikipedia